In high-pressure turbines, a small amount of air is ejected at the hub rim seal to cool and prevent the ingestion of hot gases into the cavity between the stator and the disk. This paper presents an experimental study of the flow mechanisms that are associated with injection through the hub rim seal at the rotor inlet. Two different injection rates are investigated: nominal sucking of −0.14% of the main massflow and nominal blowing of 0.9%. This investigation is executed on a one-and-1/2-stage axial turbine. The results shown here come from unsteady and steady measurements, which have been acquired upstream and downstream of the rotor. The paper gives a detailed analysis of the changing secondary flow field, as well as unsteady interactions associated with the injection. The injection of fluid causes a very different and generally more unsteady flow field at the rotor exit near the hub. The injection causes the turbine efficiency to deteriorate by about 0.6%.
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April 2010
Research Papers
Effects of Suction and Injection Purge-Flow on the Secondary Flow Structures of a High-Work Turbine
P. Schuepbach,
P. Schuepbach
Department of Mechanical and Process Engineering, LEC, Laboratory of Energy Conversion,
e-mail: schuepbach@lec.mavt.ethz.ch
ETH Zurich
, Zurich CH-8092, Switzerland
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R. S. Abhari,
R. S. Abhari
Department of Mechanical and Process Engineering, LEC, Laboratory of Energy Conversion,
ETH Zurich
, Zurich CH-8092, Switzerland
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M. G. Rose,
M. G. Rose
Institute of Aeronautical Propulsion,
University of Stuttgart
, 70569 Stuttgart, Germany
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T. Germain,
T. Germain
MTU Aero Engines GmbH
, Dachauer Strasse 665, 80995 München, Germany
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I. Raab,
I. Raab
MTU Aero Engines GmbH
, Dachauer Strasse 665, 80995 München, Germany
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J. Gier
J. Gier
MTU Aero Engines GmbH
, Dachauer Strasse 665, 80995 München, Germany
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P. Schuepbach
Department of Mechanical and Process Engineering, LEC, Laboratory of Energy Conversion,
ETH Zurich
, Zurich CH-8092, Switzerlande-mail: schuepbach@lec.mavt.ethz.ch
R. S. Abhari
Department of Mechanical and Process Engineering, LEC, Laboratory of Energy Conversion,
ETH Zurich
, Zurich CH-8092, Switzerland
M. G. Rose
Institute of Aeronautical Propulsion,
University of Stuttgart
, 70569 Stuttgart, Germany
T. Germain
MTU Aero Engines GmbH
, Dachauer Strasse 665, 80995 München, Germany
I. Raab
MTU Aero Engines GmbH
, Dachauer Strasse 665, 80995 München, Germany
J. Gier
MTU Aero Engines GmbH
, Dachauer Strasse 665, 80995 München, GermanyJ. Turbomach. Apr 2010, 132(2): 021021 (8 pages)
Published Online: January 21, 2010
Article history
Received:
August 20, 2008
Revised:
August 29, 2008
Online:
January 21, 2010
Published:
January 21, 2010
Citation
Schuepbach, P., Abhari, R. S., Rose, M. G., Germain, T., Raab, I., and Gier, J. (January 21, 2010). "Effects of Suction and Injection Purge-Flow on the Secondary Flow Structures of a High-Work Turbine." ASME. J. Turbomach. April 2010; 132(2): 021021. https://doi.org/10.1115/1.4000485
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